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In-Flight Icing Encounter and Loss of Control, Simmons Airlines, dba American Eagle Flight 4184 PDF

340 Pages·1997·3.58 MB·English
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F PB96-91040I NTSB/AAR-96/01 DCA95MA001 NATIONAL TRANSPORTATION SAFETY BOARD WASHINGTON, D.C. 20594 AIRCRAFT ACCIDENT REPORT IN-FLIGHT ICING ENCOUNTER AND LOSS OF CONTROL SIMMONS AIRLINES, d.b.a. AMERICAN EAGLE FLIGHT 4184 AVIONS de TRANSPORT REGIONAL (ATR) MODEL 72-212, N401AM ROSELAWN, INDIANA OCTOBER 31,1994 VOLUME 1: SAFETY BOARD REPORT 6486C The National Transportation Safety Board is an independent Federal agency dedicated to promoting aviation, railroad, highway, marine, pipeline, and hazardous materials safety. Established in 1967, the agency is mandated by Congress through the Independent Safety Board Act of 1974 to investigate transportation accidents, determine the probable causes of the accidents, issue safety recommendations, study transportation safety issues, and evaluate the safety effectiveness of government agencies involved in transportation. The Safety Board makes public its actions and decisions through accident reports, safety studies, special investigation reports, safety recommendations, and statistical reviews. Information about available publications may be obtained by contacting: National Transportation Safety Board Public Inquiries Section, RE-51 490 L’Enfant Plaza, S.W. Washington, D.C. 20594 (202)382-6735 (800)877-6799 Safety Board publications may be purchased, by individual copy or by subscription, from: National Technical Information Service 5285 Port Royal Road Springfield, Virginia 22161 (703)487-4600 NTSB/AAR-96/01 PB96-910401 NATIONAL TRANSPORTATION SAFETY BOARD WASHINGTON, D.C. 20594 AIRCRAFT ACCIDENT REPORT IN-FLIGHT ICING ENCOUNTER AND LOSS OF CONTROL SIMMONS AIRLINES, d.b.a. AMERICAN EAGLE FLIGHT 4184 AVIONS de TRANSPORT REGIONAL (ATR) MODEL 72-212, N401AM ROSELAWN, INDIANA OCTOBER 31, 1994 Adopted: July 9, 1996 Notation 6486C Abstract: Volume I of this report explains the crash of American Eagle flight 4184, an ATR 72 airplane during a rapid descent after an uncommanded roll excursion. The safety issues discussed in the report focused on communicating hazardous weather information to flightcrews, Federal regulations on aircraft icing and icing certification requirements, the monitoring of aircraft airworthiness, and flightcrew training for unusual events/attitudes. Safety recommendations concerning these issues were addressed to the Federal Aviation Administration, the National Oceanic and Atmospheric Administration, and AMR Eagle. Volume II contains the comments of the Bureau Enquetes-Accidents on the Safety Board's draft of the accident report. September 13, 2002 The National Transportation Safety Board adopted revisions to the findings and probable cause for this accident, as summarized below. For more information, see the full Response to Petition for Reconsideration. Findings 21, 23, 24, 25, 26, 35, and 36 (and the corresponding text on pages 177, 178, 179, 179- 80,181, 193, and 194, respectively) are revised as follows: 21. Prior to Before the Roselawn accident, ATR recognized the reason for the aileron behavior in the previous incidents and determined demonstrated that ice accumulation behind the deice boots, at an [angle of attack] sufficient to cause an airflow separation, would cause the ailerons to become unstable. Therefore, it would have been prudent for ATR to examine the combinations of icing conditions and airplane configurations that could produce the performance, stability, and control characteristics (including aileron hinge moment shifts) exhibited in the prior incidents, and the possible repercussions of such aileron hinge moment shifts had sufficient basis to modify the airplane and/or provide operators and pilots with adequate, detailed information regarding this phenomenon. 23. ATR(cid:146)s proposed post-Mosinee AFM/FCOM changes, even if which were not adopted by the DGAC and the FAA, would not have provided flightcrews with sufficient information to identify or recover from the type of event that occurred at Roselawn, and the actions taken by ATR following the Mosinee incident were insufficient. 24. The 1992 ATR All Weather Operations brochure was misleading and minimized did not adequately communicate the known catastrophic potential of ATR operations in freezing rain. 25. Information provided by ATR failed to disseminate adequate warnings and guidance to operators after the late 1980s and early 1990s about ice-related incidents did not give adequate warnings and guidance to operators about the adverse characteristics of, and techniques to recover from, ice-induced aileron hinge moment reversal events; and ATR failed to develop additional airplane modifications, which led directly to this accident. 26. Prior to the Roselawn accident, the DGAC failed to require ATR to examine the combinations of icing conditions and airplane configurations that could produce the performance, stability, and control characteristics (including aileron hinge a-1 moment shifts) exhibited in the prior incidents, and the possible repercussions of such aileron hinge moment shifts; take additional corrective actions, such as performing additional icing tests, issuing to issue more specific warnings regarding the aileron hinge moment reversal phenomenon,; developing additional airplane modifications, and providing to provide specific guidance on the recovery from a hinge moment reversal., which led directly to this accident. 35. Because the DGAC did not require ATR, and ATR did not to provide to the operators of its airplanes, information that specifically alerted flightcrews to the fact that encounters with freezing rain could result in sudden autopilot disconnects, aileron hinge moment reversals, and rapid roll excursions, or guidance on how to cope with these events, the crew of flight 4184 had no reason to expect that the icing conditions they were encountering would cause the sudden onset of an aileron hinge moment reversal, autopilot disconnect, and loss of aileron control. 36. Neither the flight attendant(cid:146)s presence in the cockpit nor the flightcrew(cid:146)s conversations with her contributed to the accident. However, aA sterile cockpit environment would probably have reduced flightcrew distractions and could have promoted a more appropriate level of flightcrew awareness for the conditions in which the airplane was being operated. The probable cause is amended as follows: The National Transportation Safety Board determines that the probable causes cause of this accident were was the loss of control, attributed to a sudden and unexpected aileron hinge moment reversal, that occurred after a ridge of ice accreted beyond the deice boots because: 1) ATR failed to completely disclose to operators, and incorporate in the ATR 72 airplane flight manual, flightcrew operating manual and flightcrew training programs, adequate information concerning previously known effects of freezing precipitation on the stability and control characteristics, autopilot and related operational procedures when the ATR 72 was operated in such conditions; while the airplane was in a holding pattern during which it intermittently encountered supercooled cloud and drizzle/rain drops, the size and water content of which exceeded those described in the icing certification envelope. The airplane was susceptible to this loss of control, and the crew was unable to recover. Contributing to the accident were 1) 2) the French Directorate General for Civil Aviation(cid:146)s (DGAC(cid:146)s) inadequate oversight of the ATR 42 and 72, and its failure to take the necessary corrective action to ensure continued airworthiness in icing conditions; 2)3)the DGAC(cid:146)s failure to provide the FAA with timely airworthiness information developed from previous ATR incidents and accidents in icing conditions, as specified under the Bilateral Airworthiness Agreement and Annex 8 of the International Civil Aviation Organization. Contributing to the accident were: 1) 3) the Federal Aviation Administration(cid:146)s (FAA(cid:146)s) failure to ensure that aircraft icing certification requirements, a-2 operational requirements for flight into icing conditions, and FAA published aircraft icing information adequately accounted for the hazards that can result from flight in freezing rain and other conditions not specified in 14 Code of Federal Regulations (CFR) Part 25, Appendics C, and 2) 4) the FAA(cid:146)s inadequate oversight of the ATR 42 and 72 to ensure continued airworthiness in icing conditions; and 5) ATR(cid:146)s inadequate response to the continued occurrence of ATR 42 icing/roll upsets which, in conjunction with information learned about aileron control difficulties during the certification and development of the ATR 42 and 72, should have prompted additional research, and the creation of updated airplane flight manuals, flightcrew operating manuals and training programs related to operation of the ATR 42 and 72 in such icing conditions. The following paragraph is removed from page 75: Hydraulically powered flight controls can overcome high control forces resulting from normal in-flight control surface hinge moments. If properly designed, they can also prevent control surface anomalies from being transmitted back through the control system and into the cockpit. According to ATR engineers, hydraulically powered ailerons were discussed during the preliminary design of the ATR 42. It was determined that adequate lateral control characteristics could be obtained without the additional weight and complexity of a hydraulic system. Hydraulic aileron control was again discussed informally among ATR engineers after an incident involving a Simmons Airlines ATR 42 in Mosinee, Wisconsin, in December 1988. ATR management has since stated that hydraulically powered ailerons have never been (cid:147)officially(cid:148) considered for either the ATR 42 or 72. The following sentence is removed from page 117: Also, with respect to Flight 4184, the chief test pilot for ATR testified that the type of roll anomaly the flight crew experienced would not have been recoverable by the average line pilot. a-3 CONTENTS EXECUTIVE SUMMARY................................................................ vii 1. FACTUAL INFORMATION 1.1 History of Flight................................................................................... 1 1.2 Injuries to Persons................................................................................ 12 1.3 Damage to Airplane............................................................................. 12 1.4 Other Damage...................................................................................... 12 1.5 Personnel Information.......................................................................... 12 1.5.1 The Captain.......................................................................................... 12 1.5.2 The First Officer................................................................................... 13 1.5.3 The Flight Attendants .......................................................................... 14 1.5.4 Air Traffic Control Personnel.............................................................. 14 1.5.4.1 DANVILLE Sector Controller............................................................. 14 1.5.4.2 BOONE Sector Controller................................................................... 15 1.5.4.3 BOONE Sector Developmental Controller......................................... 15 1.6 Airplane Information ........................................................................... 15 1.6.1 Flight 4184 Dispatch Weight and Balance Information...................... 17 1.6.2 ATR 72 Wing Design History............................................................. 17 1.6.3 ATR 72 Lateral Flight Control System Description ........................... 18 1.6.3.1 ATR 72 Directional Flight Control System......................................... 21 1.6.4 ATR 72 Stall Protection System.......................................................... 23 1.6.5 Autoflight System Description............................................................ 24 1.6.6 ATR 72 Ice and Rain Protection Systems........................................... 25 1.6.7 ATR 42/72 Type Certification History................................................ 30 1.6.7.1 General................................................................................................. 30 1.6.7.2 ATR 72 Icing Certification Program................................................... 30 1.6.7.3 Postaccident Certification Review....................................................... 35 1.7 Meteorological Information................................................................. 44 1.7.1 General................................................................................................. 44 1.7.2 Flight 4184 Dispatch Weather Information......................................... 45 1.7.3 Weather Synopsis................................................................................. 48 1.7.4 Pilot Reports (PIREPs) and Other Weather Information.................... 53 1.7.4.1 Witness Descriptions of Weather Conditions ..................................... 54 1.7.5 Hazardous In-flight Weather Advisory Service (HIWAS)................. 57 1.7.6 Information About Freezing Rain/Freezing Drizzle and General Icing Conditions.......................................................................................... 57 1.7.7 Classification of Icing Conditions....................................................... 60 iii 1.7.8 Forecasting of In-flight Icing Conditions............................................ 61 1.8 Aids to Navigation............................................................................... 63 1.9 Communications.................................................................................. 63 1.10 Aerodrome Information....................................................................... 63 1.11 Flight Recorders................................................................................... 63 1.11.1 Cockpit Voice Recorder....................................................................... 63 1.11.2 Digital Flight Data Recorder................................................................ 64 1.12 Wreckage and Impact Information...................................................... 64 1.12.1 General Wreckage Description............................................................ 64 1.12.2 The Wings............................................................................................ 67 1.12.3 Empennage........................................................................................... 71 1.12.4 Engines and Propellers......................................................................... 72 1.13 Medical and Pathological Information................................................ 73 1.14 Fire ....................................................................................................... 73 1.15 Survival Aspects .................................................................................. 73 1.16 Tests and Research............................................................................... 74 1.16.1 ATR 42/72 Lateral Control System Development History................. 74 1.16.2 Previous ATR 42/72 Incidents/Accidents........................................... 75 1.16.3 Communication of Airworthiness Information Between FAA, DGAC and ATR................................................................................. 88 1.16.4 Investigation of Lateral Control System Behavior.............................. 91 1.16.5 Postaccident NASA Icing Research .................................................... 92 1.16.6 ATR 72 Icing Tanker Tests.................................................................. 94 1.16.7 Historical Aspects of Icing Research and Aircraft Icing Certification Requirements ..................................................................................... 97 1.17 Organizational and Management Information..................................... 100 1.17.1 Simmons Airlines................................................................................. 100 1.17.2 AMR Eagle Organization .................................................................... 101 1.17.3 FAA Oversight of Simmons Airlines/AMR Eagle.............................. 103 1.17.4 FAA Partnership in Safety Program.................................................... 103 1.17.5 Simmons Airlines/AMR Eagle Pilot Training .................................... 104 1.17.5.1 General Training Information.............................................................. 104 1.17.5.2 AMR Eagle Flight Training................................................................. 106 1.17.6 Flight and Airplane Operating Manual................................................ 107 1.17.7 Unusual Attitude and Advanced Maneuvers Training........................ 117 1.18 Additional Information........................................................................ 118 1.18.1 Air Traffic Control............................................................................... 118 1.18.1.1 Chicago Area Airspace........................................................................ 118 1.18.1.2 Air Traffic Control System Command Center .................................... 118 iv

Description:
SIMMONS AIRLINES, d.b.a. AMERICAN EAGLE FLIGHT 4184. AVIONS de TRANSPORT to and operated by Simmons Airlines, Incorporated, and doing business as (d.b.a.). American Eagle flight encountered a sudden lateral jerk reaching a peak of 52 degrees bank angle. Aircraft was flying at a
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