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NASA Technical Reports Server (NTRS) 19910020938: Preliminary performance and life evaluations of a 2-kW arcjet PDF

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Iler ^ F/ 4E-(^Oy3D NASA Technical Memorandum 105149 AIAA-91-2228 Preliminary Performance and Life Evaluations of a 2-kW Arcjet W. Earl Morren and Francis M. Curran Lewis Research Center Cleveland, Ohio Prepared for the 27th Joint Propulsion Conference cosponsored by the AIAA, SAE, ASME, and ASEE Sacramento, California, June 24-27, 1991 NASA Preliminary Performance and Life Evaluations of a 2-kW Arcjet W. Earl Morren' and Francis M. Curran' National Aeronautics and Space Administration Lewis Research Center Cleveland, Ohio 44135 ABSTRACT The first results of a program to expand the operational envelope of low-power arejets to higher specific impulse and power levels are presented. The performance of a kW-class laboratory model arcjet thruster was characterized at three mass flow rates of a 2:1 mixture of hydrogen and nitrogen at power levels ranging from 1.0 to 2.0 kW. This same thruster was then operated for a total of 300 h at a specific impulse and power level of 550 s and 2.0 kW , respectively, in three continuous 100-h sessions. Thruster operation during the three test segments was stable, and no measurable performance degradation was observed during the test series. Substantial cathode erosion was observed during an inspection following the second 100-h test segment. Most notable was the migration of material from the center of the cathode tip to a ring around a large crater. The anode sustained no significant damage during the endurance test segments. Some difficulty was encountered during start-up after disassembly and inspection following the second 100-h test segment, which caused constrictor erosion. This resulted in a reduced flow restriction and arc chamber pressure, which in turn caused a reduction in the arc impedance. power processing units incorporating INTRODUCTION high-voltage pulsed starting circuits have been tested5-7. Extended, cyclic Demands for high-performance auxiliary endurance tests on both laboratory $ and propulsion systems on commercial 7 flight-type arcjet systems have been communications satellites have driven an completed. Other studies have focussed intense effort toward the development of on the impacts of arcjet system kilowatt-class arcjet propulsion systems. integration. Electron number densities This is because the performance and temperatures have been measured in advantages that these systems offer over both the near- and far-field arcjet plume existing resistojet and chemical systems using Langmuir probes9-12. The results lead to significant reductions in north- of these plume surveys have been used to south stationkeeping propellant model the effects of the slightly-ionized requirements. plumes on communications signals13,14 Testing of a flight-type arcjet system on a During the 1980's arcjet system spacecraft simulator directed toward the development has focussed on meeting the documentation of spacecraft arcjet system technology goals necessary to bring these interactions has been completed 15. The systems to flight readiness. Stable and culmination of these efforts has been the reliable operation on hydrazine selection of an arcjet system to provide decomposition products at specific stationkeeping on a new generation of impulse levels of 450 to 500 s has been commercial spacecraft16 demonstrated)-4. Pulse width-modulated • Member AIAA Copyright 0 1991 by the American Institute of Aeronautics and Astronautics, Inc. No copyright is asserted in the United States under Title 17, U.S. Code. The U.S. Govemmene has royalty-free license to exercise all rights under the copyright claimed herein for Govemment purposes. All other rights are reserved by the copyright owner. 2.0 kW. The accompanying text Future specific impulse requirements are describes the test thruster, facilities, and expected to increase, as are the limits of procedure. Also included are the results power available to spacecraft propulsion of four performance characterizations systems. Anticipating these requirements, conducted over the life of the lifetest a program was initiated to expand the thruster, as well as the details of one envelope of low-power arcjet operation interim and one post-test disassembly and beyond the current state-of-the-art inspection. (approximately 530 s mission-average at 1.6 kW into the thruster using hydrazine APPARATUS AND PROCEDURE propellant) to 600 s and thruster power levels of 2 to 5 M. The purpose of this Thruster, Figure 1 shows a schematic paper is to present the results of the first diagram of the lifetest thruster, which step toward that goal. was a modular laboratory design. The cathode was a 3.18 mm diameter 2% Arejet specific impulse is closely tied to thoriated tungsten rod with a cone of 300 the energy input per unit mass of half-angle ground on one end. The propellant expelled. Increasing the state- anode, also fabricated from 2% thoriated of-the-art specific impulse requires tungsten rod, incorporated a nozzle with a increasing the ratio of input electric power conical convergent section with a 300 to propellant mass flow rate (referred to half-angle, a 0.55 mm diameter by 0.25 herein as specific power) and/or reducing mm long cylindrical constrictor, and a the various losses inherent in arcjet conical divergent section with a 200 half- operation. Thermal, frozen flow (i.e., angle. The expansion area ratio was 214. energy not recovered as thrust), and Figure 2 shows an exploded view of the nozzle losses are dominate factors in cathode tip/anode constrictor region. The arcjet efficiency. An investigation into arc gap (the minimum axial distance means of reducing thermal losses is under between the cathode tip and the anode) way17 and an earlier effort showed that was set to 0.58 mm. This was increasing nozzle expansion ratio accomplished by inserting the cathode increased thruster efficiencytg. Additional into the thruster until it met the anode, near-term programs are attempting to then withdrawing it by the desired gap reduce frozen flow losses. This effort setting. The electrodes were contained in seeks to enhance specific impulse by a housing fabricated from titaniated- increasing the specific power. zirconiated-molybdenum (TZM). The anode housing had a 0.25 mm thick layer The first step toward expanding the of molybdenum powder plasma-sprayed operating envelope beyond the current onto the exterior surface to enhance its state-of-the-art was to identify the life- emittance. limiting issues in the current thruster technology at conditions beyond those The joint between the anode and the typical of low-power arcjets. To this end housing was a tapered interference fit a modular laboratory model arcjet thruster 6.35 mm in length with a 50 half-angle was run for a total of 300 h in three and a minor diameter of 13.7 mm. This continuous 100-h test segments at joint was lapped during thruster assembly constant specific impulse and power to aid thermal conduction from the anode levels of 550 s and 2.0 kW, respectively, to the housing and to minimize gas on a mixture of hydrogen and nitrogen leakage. A TZM injector disk was located simulating hydrazine decomposition immediately behind the anode. Two 0.38 products. Performance was measured at mm diameter holes in the disk injected the propellant mass flow rates ranging from propellant into the are chamber, the small 3.0x10-5 to 5.0x10-5 kg/s and thruster plenum surrounding the cathode tip, so as input power levels ranging from 1.0 to to set up a vortex flow field. This was 2 done because a vortex flow has been number 10 stainless steel bolts. Graphite shown to improve starting and steady foil gaskets sealed this joint. Figure 3 state stability. However, no systematic shows a photograph of this design prior study has yet been conducted to evaluate to assembly. the effects of vortex strength on arcjet stability. During operation, propellant was fed to the thruster propellant feedthrough. The Behind the injector disk was a boron gas flowed over the spring, through nitride insulator (the front insulator in several axial channels in the boron nitride figure 1). The front insulator served to ram and into a plenum between the front provide electrical isolation of the cathode and rear insulators. From there the gas from the anode-potential housing; to force flowed through sixteen axial channels, the gas flow through several axial approximately 0.5 mm square in cross- channels located next to the housing wall; section, cut into the outer surface of the and to transmit the compressive force front insulator. This placed the gas in imparted by the spring, located in the rear direct contact with the housing and half of the thruster, to the front provided some regenerative cooling of the insulator/injector and injector/anode forward end of the thruster. The gas then joints. The compressive forces on the flowed through two 0.381 mm diameter joints around the injector were required to holes in the injector disk and into a small assure that the propellant flowed through plenum around the cathode tip (the arc the injector ports and not around the chamber). The gas was injected into the injector. Flowing the propellant next to are chamber so as to set up a vortical the anode housing wall provided some flow. The gas then passed through the regenerative cooling of the anode region. constrictor where it is heated by the arc and is accelerated in the nozzle, The upstream end of the thruster was producing thrust. contained in the boron nitride rear insulator. The propellant and cathode Propellant. The propellant used was a feedthrough fittings were commercially- mixture of hydrogen and nitrogen at a available compression fittings modified to mixture ratio of 2:1 by volume, mate with flats machined into the rear simulating hydrazine decomposition insulator. These joints were sealed with products. The pure (99.99% minimum) gaskets made from 0.25 mm thick gases were stored in high-pressure graphite foil. An inconel spring located bottles, then metered separately and within the rear insulator provided the mixed upstream of the thruster. The compressive force necessary to prevent mixture entered the thruster at room leakage around the injector disk while temperature. allowing for thermal expansion of the internal thruster components. A boron Power Processing. Power was supplied nitride plunger transmitted the to the thruster from a pulse width- compressive force to the front insulator modulated power processing unit (PPU) which in turn pushed the injector disk with high-speed current regulation. The against the rear of the anode. Graphite PPU was capable of delivering up to 130 foil gaskets between the front insulator, Vdc and 50 A to the thruster. Starting the injector disk, and the anode prevented was facilitated by a built-in, high-voltage gas from blowing by the injector disk. circuit capable of providing a 4 kV pulse Note that it was necessary for the front every second until breakdown occurred. insulator to slide freely over the cathode Starting current surge protection kept the within the anode housing for it to PPU from delivering maximum current effectively transmit the springs force to until the arc had sufficient time to blow the injector joints. The rear insulator was through the constrictor, seating in the clamped to the anode housing by two 1.6 nozzle divergent section. Earlier efforts to mm thick molybdenum flanges and four start without this surge protection often 3 resulted in constrictor damage due to transducer signals into engineering units, momentary spot attachment in high- as well as calculation of several derived pressure regions upstream of the parameters. These data were then constrictor at high current levels. Further displayed in digital and graphical forms details of this PPU have been detailed on the computer screen at a sampling rate elsewhere19. of about 1.5 Hz. This system also controlled automatic shutdown of the Test Facilities. Two test facilities were thruster power and propellant flow in the used to carry out these experiments. All event any monitored parameters deviated performance characterizations were from designated ranges. This permitted conducted in a cylindrical vacuum tank unattended operation of the thruster. measuring 1.5 m in diameter by 4.5 m long. This tank was equipped with four The arc voltage was measured at the 0.8 m diameter oil diffusion pumps power leads connecting the PPU to the backed by a lobe-type blower and two test facilities. The are current was rotary piston roughing pumps. The test measured using a shunt in series with the cell background pressure was below 0.1 thruster. The current signal was Pa for all performance tests. During processed using a low-pass analog filter operation in this facility the thruster was with a time constant of about 0.5 s. The mounted on a thrust stand in a horizontal filter was necessary to obtain a do-level orientation, on the axis of the vacuum signal because the current had about 5% tank. Figure 4 shows a photograph of an ripple at 20 kHz. Both voltage and arcjet operating in the performance test current signals were then fed to the facility. DACS through isolation amplifiers. The DACS responses to the voltage and Figure 5 shows a photograph of an arcjet current inputs were calibrated by mounted in the endurance test facility, a removing the PPU from the electrical cylindrical vacuum chamber 0.5 m in circuit, then applying reference voltages diameter by 0.6 m high. This test cell was and currents to the signal conditioning equipped with a rotary piston roughing system from a laboratory do power pump capable of maintaining test cell supply. pressures of approximately 100 Pa during all endurance tests. During operation in Propellant mass flow rates were this facility the thruster was mounted in a measured using commercially-available vertical axis orientation and fired directly thermal conductivity-type mass flow into the inlet of the pumping system. meters with operating ranges of 0 to 10 SLPM. These units maintained steady Operational parameters monitored during propellant mass flow rates by using flow all tests included arc voltage and current, sensor feedback to control integral hydrogen and nitrogen mass flow rates, solenoid-operated flow control valves. propellant feed pressure, and temperature The mass flow controllers were calibrated of the exterior of the anode housing. in-situ at each of the test facilities using a Thrust was measured only during volumetric standard, as is common performance characterization. All data practice in the flow measurement were monitored, reduced, displayed, and industry. The individual gases were stored using a microcomputer-based data flowed through the respective mass flow acquisition and control system (DACS). controllers, then into a cylinder of known Data were stored every 30 seconds volume. The pressure and temperature in throughout the endurance tests. The the cylinder were measured before and performance and endurance test data after flowing gas into the cylinder, and acquisition programs were written using a the length of time gas flowed into the graphically-driven software system which cylinder was recorded. The mass added facilitated real-time reduction of all to the cylinder was then calculated assuming ideal gas behavior. This 4 standard had an estimated uncertainty of about 1%, with typical repeatabilities Test Procedure. The objective of this test better than M. series was to identify the life-limiting issues of arciet thruster operation at a Thrust was measured by a calibrated specific impulse and power level of 550 s displacement-type thrust stand designed and 2.0 kW, respectively. The approach and fabricated at the NASA Lewis was to conduct a series of 100-h Research Center. This unit was equipped endurance tests with intermittent thruster with numerous water cooling passages performance characterizations and throughout the structure to minimize physical examinations. Figure 6 shows thermal drift due to component expansion the test chronology time line. Prior to during thruster operation. Thermal drift assembly the electrode masses were was observed to be less than 1% of the recorded. The constrictor dimensions nominal thrust level during all tests, and were determined by making a mold of the was found to be always in the direction of constrictor region using a vinyl- decreasing thrust. Therefore, all thrust polysiloxanc analogue (dental putty), then measurements were corrected by inspecting the mold under a microscope recalibrating the thrust stand while hot, equipped with a three-axis translation making any residual thrust measurement stage assembly. The length of the anode error conservative. Additional details of protruding from the end of the anode this thrust measurement system are housing was also recorded. available elsewhere20. Immediately following assembly the The propellant feed pressure to the thruster was installed in the endurance thruster was monitored using a strain- test facility for a 20-h burn-in period. gage type pressure transducer with a Laboratory experience has demonstrated range of 0 to 1.4 MPa. It is important to the tendency with a new cathode for the note that the measured pressure is that of arc voltage to increase substantially over the propellant upstream of the injector the first 20 to 30 h of operation at disk, which was estimated to be constant mass flow rate and current. The substantially higher than the arc chamber purpose of the burn-in period was to pressure. Furthermore, the pressure drop bring the electrode to a condition more across the injector disk was a function of representative of steady state prior to the thruster operating conditions. initial performance characterization of the Nonetheless, the feed pressure was thruster. During most of this phase of useful as an indication of the integrity of testing the thruster was operated at a flow the flow path and pressure vessel during rate of 5.Ox 10-5 kg/s and a power level of operation. 1.5 W. The last several hours of burn-in included operation at 1.75 and 2.0 kW, The temperature of the anode housing also at a mass flow rate of 5.0x10-5 kg/s. surface (see Fig. 1 for location) was measured using a two-color optical Following burn-in, the thruster was pyrometer with a range of 700 to installed on the thrust stand to 14000C. This device used the ratio of the characterize thruster performance. This energy emitted at two wavelengths (both was done to provide a baseline for interim in the vicinity of 1 p m) to calculate the and post-test comparison, and to aid in selecting the mass flow rate for the target surface temperature. The output endurance test. As shown in Table I, reading was not sensitive to the absolute performance was measured at each of value of the emittance, but to the slope of the variation of emittance with three mass flow rates (3.Ox 10- 5 , wavelength. 4.0x10-5 , and 5.0x10-5 kg/s) at up to 5 power levels (1.0, 1.25, 1.5, 1.75, and 2.0 kW). The boundaries of the operating 5 envelope were defined by a PPU output were cancelled. The thruster was voltage limit of 130 V and an anode disassembled a final time, after which the housing temperature limit of 1400°C. electrodes were sectioned for metalographic analyses. Following the initial performance characterization, the thruster was installed RESULTS AND DISCUSSION in the endurance test facility and run for 100 h at a power level and specific Performance Characterizations. Table II impulse of 2.0 kW and 550 s (nominal), summarizes performance data acquired respectively. Due to the current-regulating during this test series. Figure 7 shows the nature of the power supply, it was measured specific impulse versus specific necessary to reduce the current setpoint power (i.e., the ratio of electric power to occasionally during the endurance tests to mass flow rate) for the test thruster maintain a constant 2.0 kW as the arc following the 20-h burn-in period. These impedance increased with time. At the data (labelled "0 h" in Table 11) provided end of the first 100 h, the thruster was a baseline against which to measure any reinstalled on the thrust stand and changes in thruster performance during characterized to document any the course of the endurance test series. performance changes. After the 100-h This test also showed that the mass flow performance check the thruster was rate necessary to obtain the specified moved back to the endurance test facility endurance test condition of 550 s at a where it was run another 100 h at 2.0 kW power level of 2.0 kW was 5.0x 10-5 and 550 s. Upon completion of the kg/s. Note that the specific impulse at a second 100-h test segment, the thruster given specific power was dependent upon performance was checked, following mass flow rate. This has been observed which it was disassembled for inspection. previously in lower-power arcjets21. To date there are insufficient data to The third 100-h test segment was understand this phenomenon. Also preceded by a performance shown in Fig. 7 are performance data characterization. For reasons which will obtained in previous arcjet tests2.21,22. be discussed later, graphite foil gaskets Agreement with the data of the current were not used in the injector disk seals effort is generally good. The Ref. 2 data during this test segment. An anomaly were acquired at two different test during the first restart resulted in some facilities. The uppermost point was constrictor damage. This necessitated measured in an industrial test cell at a another disassembly and inspection, mass flow rate and power level of during which the surfaces of the injector 4.4x10-5 kg/s and 2.0 kW, respectively, disk were cleaned and the inconel spring using hydrazine propellant. The other was stretched to increase the preload on Ref. 2 datum was measured at a the injector seals. The performance government facility at 2.8x10-5 kg/s and characterization was then completed and a 1.0 kW on a 2:1 hydrogen-nitrogen third 100-h test segment was conducted. mixture. Although the Ref. 21 data were obtained at a variety of mass flow rates, After completing a total of 300 h at the they were all measured at specific power nominal operating conditions the thruster levels below 15 MJ/kg. At that point the was disassembled for inspection a second effects of mass flow rate variations on time. No performance characterization specific impulse began to disappear. The was performed prior to this inspection. Ref. 22 data were measured at LeRC on a The thruster was reassembled after the hydrogen-nitrogen mixture at a mass flow electrodes were examined so that the rate of about 4.1x10-5 kg/s. Both points performance could be measured. are within approximately 3% of the However, starting difficulties were 4.0x 10-5 kg/s data acquired during the encountered, and the performance tests current effort. Other performance data at 6 comparable conditions indicate good later in this section. The second and third agreement as well18,23 unintended shutdowns occurred after approximately 173 and 230 h of thruster Figure 8 shows the results of the operation, respectively. In each case a performance characterizations conducted facility interlock for the thruster power during the test series at a flow rate of supply was violated, causing a loss of 5.Ox 10-5 kg/s. Figures 9 and 10 show the power to the PPU. The test was restarted corresponding performance at flow rates within about 45 minutes of the second shutdown, and immediately following the of 4.Ox 10-5 kg/s and 3.Ox 10-5 kg/s, third shutdown. Each time the thruster respectively. No degradation of thruster restarted without difficulty. Neither of performance is indicated at any of the these shutdowns was caused by any operating conditions tested. This is parricularly interesting in consideration of irregularity in thruster operation. an anomaly experienced during the first The arc voltage increased during the first restart of the thruster after the 200-h disassembly and inspection. An apparent 200 h of operation at an average rate of 35 mV/h. As shown in Fig. 11, the leak around the injector disk resulted in thruster experienced periods of increasing substantial erosion of the constrictor. and decreasing voltage, although all This caused the arc chamber pressure at a voltage values fall within a band of ±2.5 given mass flow rate and power level to V from the nominal value at that point in decrease, which lead to a decrease in arc the test. This represents a variation of impedance at all operating conditions. Further details of this anomaly will be about 2.2% of the average arc voltage given in a later section. The most measured during the first two 100-h test segments. Arc voltage fluctuations of this important result was that thruster performance and stability were not magnitude have been observed in impacted by the constrictor damage. previous endurance tests8,23. During the third 100-h test the voltage rose at a Endurance Tests, Figures 11, 12, and 13 substantially lower rate. This test segment show the are voltage, propellant feed was also relatively free of the voltage pressure, and anode housing temperature, excursions typical of the first two respectively, at 30-second intervals over endurance tests. However, the voltage the endurance test series. As discussed during this test was several volts lower earlier, the test plan called for a series of than during the first two test segment due 100-h continuous endurance test to the constrictor damage sustained prior segments with intermittent performance to this test segment. characterizations and physical examinations. Three unscheduled During most of the endurance tests the shutdowns also occurred, one during propellant feed pressure remained steady. each of the 100-h test segments. The first There were two instances, however, occurred about 20 h into the first test, when the feed pressure declined gradually caused by interruption of the two-color over periods of about 20 h and 50 h pyrometer signal to the DACS. This during the early portions of the first and violated the lower shut down setpoint for second test segments, respectively (see this parameter, which in turn shut down Fig. 12). Either of these trends could the propellant flow and PPU. The test have indicated a leak from the thruster was restarted after about one hour pressure vessel, an increase in constrictor without difficulty. None of the thruster diameter, or a leak past the injector disk operating parameters was out of its into the arc chamber. The most serious specified range prior to this shutdown, leak would be from the thruster pressure although a declining feed pressure trace vessel because this would have been a (see Fig. 12) was causing some concern. failure resulting in the loss of This will be discussed in greater detail performance and, perhaps, the failure of 7 the thruster. Concurrent symptoms of a 630 kPa. Between 100 and 135 h the pressure vessel leak would have been voltage fell from an initial value of 112 V declining arc voltage and increasing to a minimum of about 110 V and the anode housing temperature (due to an anode housing temperature rose to a increase in the effective specific power). maximum of nearly 1400°C. These The symptoms of an increase in trends suggested the possibility of a leak constrictor diameter are similar to those of from the thruster pressure vessel or a leaking pressure vessel: concurrent constrictor erosion. However, the voltage decreases in arc voltage and feed began a strong recovery and the anode pressure. Leakage past either of the housing temperature fell sharply at about injector disk seals would have allowed 135 h, while the feed pressure was still propellant to bypass the two injector falling. At about 150 h the feed pressure ports. This would result in a reduction in and arc voltage increased in a step change feed pressure, accompanied by irregular to 680 kPa and 115 V, respectively. The arc voltage excursions, although no arc voltage, feed pressure, and anode general trend toward decreasing arc housing temperature were relatively voltage would be expected. The arc steady during the remainder of the second voltage excursions could be due to rapid test segment. movement of the arc seat about the cathode tip in the absence of sufficient Thruster Inspections. As shown in Fig. vortex stabilization in the arc chamber. 6, the thruster was disassembled for inspection following the second 100-h During the first 20 h of the first 100-h test endurance test. The overall thruster length segment the feed pressure gradually was measured prior to disassembly. This decreased from its original value of 680 was necessary for determination of the kPa to about 640 kPa. Over the same arc gap later in the disassembly. The period the anode housing temperature overall length was found to have increased by about 30°C to 1330°C and increased by about 0.56 mm. The length the arc voltage remained steady at 109 V. of portion of the anode protruding from Following the first unintended shutdown, the anode housing was also measured. the feed pressure and the anode housing The anode had moved within the tapered temperature returned to their original seat in the anode housing as indicated by values of 680 kPa and 1330°C , a 0.56 mm increase in the length of the respectively. At that time it was protruding portion. Because the cathode speculated that the front insulator might was tied rigidly to the rear of the thruster, have been sticking to the cathode or movement of the anode within the anode housing prior to the shutdown. housing would result in an increase in the This would have defeated the spring in arc gap. The movement of the anode the rear of the thruster, allowing the within the anode housing could have compressive force on the injector seals to contributed to the pressure variations be relieved, and resulting in leakage past observed during the first two test the injector. The thermal cycle associated segments by allowing propellant to leak with the shutdown could then have freed past the tapered seal or by relieving some the insulator, allowing the thruster to of the compressive force on the injector return to its original condition. No seals. significant pressure variations were encountered for the remainder of the first The arc gap was determined by 100-h test segment. measuring the overall thruster length with the cathode pushed in until it met the During the first half of the second 100-h anode, then subtracting this length from test. The feed pressure gradually the overall length measured previously. decreased from an initial value of The are gap was found to have increased approximately 680 kPa to a minimum of by 0.013 mm, which was about 0.55 mm 8 less than was expected based on the cracks. Differences in the operating increase in the length of the anode histories of these two cathodes include a protruding from the housing. lower are current and anode temperature (by at least 4000C), and substantially The discrepancy between the measured greater number of starts on this cathode arc gap and the forward movement of the than that of the current work. anode within the housing was explained when the cathode was removed from the Inspection of the graphite gasket between thruster for inspection. The tip of the the insulator and the injector disk revealed cathode had formed a crater nearly 1.3 some holes, although the actual sealing mm in diameter with a bulged rim (see surface was intact. However, the gasket Fig. 14). The material on this rim lay between the injector disk and the anode outside the original conical envelope by had been completely consumed, leaving an amount approximately equal to the no visible trace. This had been observed distance moved by the anode. The axial in a previous life test conducted by the distance from the original tip location to author during which the anode had the crater rim was approximately 0.58 operated at temperatures some 500°C mm. Figure 15 shows a sketch of the higher than in the current tests. As was cathode tip with the original conical tip discussed earlier, some degradation of the shape superimposed for comparison. Of injector sealing was believed to be particular interest was the migration of responsible for the pressure fluctuations material from the center of the cathode tip observed during the first two 100-h to a region outside the original conical endurance tests. The lack of any remnants shape of the cathode tip. This could have of the forward graphite foil gasket resulted in shorting of the cathode to the confirmed those suspicions. Of particular anode had the anode not moved forward interest was the fact that the thruster within the housing. The measured resumed stable operation after each of the cathode mass loss was approximately pressure excursions, suggesting that the 2x 10-6 kg. graphite foil gaskets were unnecessary components. Figure 5a of reference 24 shows a cross section of a 2% thoriated tungsten The anode was not removed from the cathode tip operated for 9 h in three housing at this time to avoid disturbing thermal cycles at a current of 11 A. The the tapered seal between these two overall diameter of the crater in that components. However, examination of cathode tip was only about 0.5 mm the constrictor exit under a microscope (versus 1.3 mm for the current revealed no substantial degradation. specimen). However, the movement of Some metal deposits lined the nozzle wall material to a region outside the original near the constrictor exit, but the conical shape of the tip bears a striking constrictor was still circular and its resemblance to the current test results. diameter had increased by only 0.015 mm This suggests that the observed cathode (to 0.57 mm). erosion was driven by some phenomenon which was not time dependent. The thruster was reassembled and its performance was characterized in The tip of another cathode run for a total preparation for a third 100-h test of 1000 h and 500 thermal cycles at a segment. The only deviation from constant current of 11 A displayed a previous thruster assembly procedures distinctly different type of erosion$. The was the deletion of graphite gaskets results of that test showed a crater slightly around the injector; this in an effort to smaller than that of the current test, but return the thruster to a condition as close the rim of the cathode was not bulged. as possible to that prior to the Instead, the crater rim had several axial disassembly. The arc gap was set to 0.60 9

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